Hey guys, my bad for not keeping this up to date for a while..
The car has been finished since last week, but had an coolant leak so figuring this out at the moment.
I think it's because the end of my coolant pipe had a flat spot. (i should have made a bead on it but heck i'm gonna try making it round without the bead first so i don't have to take the manifold and turbo off again lol.)
Car runs great so far but no logs yet.
Also tried routing an airfilter and this worked out.
So i had to change my waterpipe.
Only ran a MHD pump backend and what i could tell from keeping an eye on my jb4 gauges it stayed nice around it's target so there was no boost issues with the wastegate position and full boost was at 4000 RPM.
And holy cow that open dump is
loud!
I'll post some logs and videos when my car isn't losing coolant anymore.
Here are some pics tho..
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