I have to say v8bait is amazing he was right on point I know everyone said my wgdc was good but for new turbos was high and I couldnt figure out prob. Well i got 2 recalls done and bmw commented that my inlets didnt fit with my outlets I never thought to check they apparently couldnt get my inlet lined up with front turbo, they scratched crap out a my inlet and it wasnt attached so it must been partially blocking my turbo ,justin saved my engine cause if wasnt for him saying anything I would have never noticed. A lesser man would have taken my money and ran leaving me with a perfectly acceptable tune my wgdc now sits at about 5 lower from 6k to 7k also my stft are perfect again
Edit fml stft still deviating at redline hopefully needs to re adapt
Edit fml stft still deviating at redline hopefully needs to re adapt
Last edited: